My BX has returned with a shiny new MOT. There were a few advisories, such as the indicator repeater not working evidently solved by giving the dash a thump. One of the rear wheel bearings is grumbling, most of the bulbs in the dash, have failed, the heater is stuck on hot, and the rear door needs building back up. So the first job was to clean it of the 4 years of leaves, and cobwebs inside, and giving the outside a good wash.
Not saying I was keen to get it legal, but a 00:05 on the 1 July, I taxed it. So it is now back on the road. Happy days.
Ian's BX 16TGS. Now gone.
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Meter rat
- Confirmed BX'er
- Posts: 74
- Joined: Sun Jul 09, 2017 10:52 am
- Location: Between Derbyshire and Argyle and Bute
- My Cars: Citroen Acadiane
Citroen BX 16 TGS
The moderns.
Skoda Superb
Citroen C1
The Motor Bike,
250 MZ - x 16
Re: Ian's BX 16TGS. Now gone.
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panky
- BXpert
- Posts: 675
- Joined: Mon Jan 22, 2018 4:44 pm
- Location: Widnes
- My Cars: 1985 BX 19 GT (DKK), 1971 Morris Minor Traveller, 1971 Commer Auto-Sleeper, 1969 Commer Jennings Roadranger.
'88 BX GTi (a long time ago) - x 171
Re: Ian's BX 16TGS. Now gone.
Excellent, I'm sure you've got plenty of work lined up for it 
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Meter rat
- Confirmed BX'er
- Posts: 74
- Joined: Sun Jul 09, 2017 10:52 am
- Location: Between Derbyshire and Argyle and Bute
- My Cars: Citroen Acadiane
Citroen BX 16 TGS
The moderns.
Skoda Superb
Citroen C1
The Motor Bike,
250 MZ - x 16
Re: Ian's BX 16TGS. Now gone.
Today was a case of two steps forward three backwards. One of the reasons why I took the BX off the road, was due to the rear drivers side passenger window falling down into the door interior. So some aluminium glass runners were obtained from Chevronics. These were fitted for the MOT. So today was a visit to the Men’s Shed, where space had been booked on the ramps. First job was to remove the remaining pieces of moisture barrier.
Using a permanent marker, a new moisture barrier was marked out, and being a dumb twit, I still managed to get it wrong.
A few corrective measures were taken and we had a new moisture barrier.
While this was setting up, the door cloth was glued back into place where it had come adrift.
Once this had set, the door was built up. I now had a complete door, with a working window.
The next job was to investigate why the heater was on permanently. This involved stripping down the heater controls. This turned out to be due to the outer cable having come out of its clamp. I managed to get in once, but when tested, and it got close to cold, it pushed out again. At least the heater valve appears not to be seized. Loosing the will to live with trying to get this to work, I opted to fit some new bulb in the heater controls, and rework the fan control so it can operate at full speed.
Most of the centre console is now in the boot. Whilst waiting for the door card, and moisture membrane to dry, I knackered up the boot light.
I also refitted the trim behind the drivers side rear door. Which had come adrift.
I also refitted the trim behind the drivers side rear door. Which had come adrift.
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